3 in the green
Line Up and Wait
I'll get right to it...
New/first owner here. '53 C170B with an O-300A and a 7653 prop. Overhauled early 2017, ~270 hrs SMOH. Prebuy and ~16 hour ferry over and ran smooth like an O-300 should.
First flight at new home and takeoff is anemic, climb-out less than stellar, and noticeable (but not terrible vibration). Not stumbling or coughing, but vibration and less than full power. Static runup not too far off, about 2,200, on the low side. At first, vibrations only present themselves at higher (1,500+) rpm, then as engine warmed up the vibrations worsened to a degree and also were noticeable at lower rpm. Mag checks are perfect, 50-75 rpm drop, no difference between the two.
A few other facts (clues?):
-previous owner ran mogas a lot, or a blend with 100LL
-now since being ferried it's 100% 100LL
-fuel selector rebuilt on the ferry flight over as it started leaking
-annual was completed early March as part of my pre-buy and new carb, left mag, timing set, intake gaskets as there was a leak there
I'm thinking maybe a slightly sticking valve? Would a switch to 100LL cause this so soon?
New/first owner here. '53 C170B with an O-300A and a 7653 prop. Overhauled early 2017, ~270 hrs SMOH. Prebuy and ~16 hour ferry over and ran smooth like an O-300 should.
First flight at new home and takeoff is anemic, climb-out less than stellar, and noticeable (but not terrible vibration). Not stumbling or coughing, but vibration and less than full power. Static runup not too far off, about 2,200, on the low side. At first, vibrations only present themselves at higher (1,500+) rpm, then as engine warmed up the vibrations worsened to a degree and also were noticeable at lower rpm. Mag checks are perfect, 50-75 rpm drop, no difference between the two.
A few other facts (clues?):
-previous owner ran mogas a lot, or a blend with 100LL
-now since being ferried it's 100% 100LL
-fuel selector rebuilt on the ferry flight over as it started leaking
-annual was completed early March as part of my pre-buy and new carb, left mag, timing set, intake gaskets as there was a leak there
I'm thinking maybe a slightly sticking valve? Would a switch to 100LL cause this so soon?