JimNtexas
Pattern Altitude
- Joined
- Dec 21, 2006
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- 2,259
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- Austin, Texas
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Jim - In Texas!
Quite an eery coincidence that the aircraft flew 261 flights before the part failed.The FAA described the legal fall out of the investigation: "Aircraft N407NV flew a total of 261 revenue flights (See IOP #26) before the nut backed off of the elevator power control boost cylinder rod end and caused the loss of pitch control that resulted in the aborted takeoff on August 17, 2015. Had the nut fallen off while the aircraft was actually flying, or had the crew not aborted the takeoff, the maintenance and inspection complacent actions performed by AAR Aircraft Services personnel would have resulted in an aircraft flying without the ability to control its pitch attitude, as evidenced by the aborted takeoff flight control response experienced by the crew on N407NV. Deliberate acts of noncompliance by company personnel resulted in improper maintenance that endangered numerous lives and properties during 261 subsequent flights following its return to service by AAR Aircraft Services, Inc., caused an unacceptable safety risk to safety and caused the airline to be in violation of 14 CFR. Part 121.369(b)(1)." Following the receipt of a response by AAR stating that the maintenance steps had been completed including the last steps 28 and 29, the FAA thundered: "This confirms that they are even now, still not familiar or do not intend follow the Allegiant Air GMM procedures for documenting Forms M301 and M302 specifically requires maintenance personnel to enter partial work to be entered in the Partial Work Accomplished sections of the form as indicated in GMM Page 21.2.19.1Section B items 4 and 5 (See IOP 21B), which the repair station is required to follow. Additionally, in the response from AAR Aircraft Services, Inc., on page 3 paragraph 2, they state and admit that they have had the same quality escape two other times. This shows these quality lapses are likely systemic, and yet the repair station shows angst over not being allowed to self-disclose a recurring concern."
261 flights eery coincidence.....Alaska261.Here's another article.
http://avherald.com/h?article=48b6fd53&opt=0
Quite an eery coincidence that the aircraft flew 261 flights before the part failed.
Yeah. If the part had failed in flight the result would have been very similar.261 flights eery coincidence.....Alaska261.
In Alaska the elevator was jammed. Here it wasn't jammed, just not getting input from the yoke. What do you think the chances are they could have managed it enough with power, trim, flaps, slats, maybe even spoilers to at least have an outcome no worse than United's DC10 in Iowa?Yeah. If the part had failed in flight the result would have been very similar.
It's a total coincidence, but an odd one nonetheless
They weren't exactly the same failure, but still would have produced similar pitch control issues in flight.In Alaska the elevator was jammed. Here it wasn't jammed, just not getting input from the yoke. What do you think the chances are they could have managed it enough with power, trim, flaps, slats, maybe even spoilers to at least have an outcome no worse than United's DC10 in Iowa?
Or, just as likely, they were kicker OUT of the airlines.After working with some very substandard A&Ps I would imagine some of these made their way into the Airliners.
Yeah. That was no accident. Somebody in the trenches got tired of the bs.I like how the article says the report was 'accidentally' sent to the Times.
I have a funny feeling that wasn't an accident.
Maybe Allegiant is great at the paperwork side of it, and that's keeping the FAA from digging any deeper.
. I spent some time as the Chief Pilot of a charter company, and while working with the FAA I learned that 99% of being in compliance was making sure the paperwork was right. The FAA didn't have the manpower to actually *ensure* we were flying our airplanes on the up and up, but as long as I can point to paperwork which showed that we were coloring inside the lines, they took our word for it..
Isn't the FAA too busy trying to find new ways to increase the cost of flying light airplanes to have time to worry about the big iron?
Perhaps I'm naive, but I'd be surprised if the FAA was intentionally covering up known safety issues. I spent some time as the Chief Pilot of a charter company, and while working with the FAA I learned that 99% of being in compliance was making sure the paperwork was right. The FAA didn't have the manpower to actually *ensure* we were flying our airplanes on the up and up, but as long as I can point to paperwork which showed that we were coloring inside the lines, they took our word for it.
I feel like something similar might be happening here. Maybe Allegiant is great at the paperwork side of it, and that's keeping the FAA from digging any deeper.
Alaska 261 was the horizontal stab trim jackscrew failure.Alaska's was initially jammed…..until it finally broke completely.
Why? Because of the free cremation?The only time I would fly Allegiant, Spirit or Frontier is in my casket on the way home.
Spares. I don't see any maintenance vehicles out there.I frequent KPIE all the time, (Clearwater Airport). I see the Allegiant airplanes on the grassy area lined up all the time.
View attachment 53714
Maintenance stops by but I always wondered how extensive can the repairs be outside...95 degrees...100% Humidity. I rather take my chances with Thug United!!
Trying hard to be less burdensome. . . Good God! Is that a serious comment? We're supposed to be grateful that an unaccountable bureaucracy, that can't get out if it's own way, has decided to only punch us in the face six times an hour, instead of ten?Seriously? If you believe that then you really have no idea. Consider the following:
Part 23 rewrite.
NORSEE policy
The recent STCs issued to the EAA.
Light sport
The new compliance philosophy
and there's more.
The FAA has been trying very hard to be less burdensome on GA and has made great strides in this area. Not sure where you get your ideas.
Why? Because of the free cremation?
Ron Wanttaja
Trying hard to be less burdensome. . . Good God! Is that a serious comment? We're supposed to be grateful that an unaccountable bureaucracy, that can't get out if it's own way, has decided to only punch us in the face six times an hour, instead of ten?
I imagine you're working hard at FAA, and grant you that - but working hard isn't the same as working smart. . .is everything the FAA touches a crater? No, some good stuff happens, and there have been ATC folks I'd like to buy a beer - a lot them, actually, and very few I'd like to slap, for sure. But the accountability is NOT there - it's at such a far remove from the aviation community as to be, well, like the IRS is to tax payers. Only FAA is better funded. . .