Steve
En-Route
As some of you know, my plane has been grounded since March for an engine overhaul and a wing tank skin replacement. Suffice it to say both took longer than promised.
I took advantage of the downtime as best I could by refurbishing the plane from the firewall forward. It may not sound like a lot but when you're basically a one man show the acts run pretty long to get in all the bit parts.
I've posted a few pictures taken during the project in an album on PoA. If you go to my profile you should be able to find a link to it. The images were selected fairly at random for posting, but I think you'll get an appreciation of the scope of work involved. I was fortunate to have a couple of experienced mechanics to refer to for some limited technical advice.
Almost 8 months to the day (actually a couple of days over) I last cranked the engine the starter engaged again. I did the post-overhaul break-in ground run late on Friday (10/16/09), too late to follow up with the initial post-overhaul flight test which now probably won't happen until the middle of next week due to other commitments. As far as the first engine run went, the only thing I noted that needed adjustment was the throttle linkage that stopped at 900 RPM at idle position instead of the expected 800 RPM. A few turns on a throttle linkage rod end fork fixes that.
Sorry, Pete, but the album image count limit was 60...
I took advantage of the downtime as best I could by refurbishing the plane from the firewall forward. It may not sound like a lot but when you're basically a one man show the acts run pretty long to get in all the bit parts.
I've posted a few pictures taken during the project in an album on PoA. If you go to my profile you should be able to find a link to it. The images were selected fairly at random for posting, but I think you'll get an appreciation of the scope of work involved. I was fortunate to have a couple of experienced mechanics to refer to for some limited technical advice.
Almost 8 months to the day (actually a couple of days over) I last cranked the engine the starter engaged again. I did the post-overhaul break-in ground run late on Friday (10/16/09), too late to follow up with the initial post-overhaul flight test which now probably won't happen until the middle of next week due to other commitments. As far as the first engine run went, the only thing I noted that needed adjustment was the throttle linkage that stopped at 900 RPM at idle position instead of the expected 800 RPM. A few turns on a throttle linkage rod end fork fixes that.
Sorry, Pete, but the album image count limit was 60...