Matthew
Touchdown! Greaser!
I came across this today. The full report is in the PDF.
"Undetectable damage" to the aircraft prevented it from being able to fly. The Captain didn't realize it until he tried to rotate, then shut her down. His checkpilot scolded him for aborting above V1, but didn't try to override. They went off the end of the rwy.
Later inspections and wind tunnel simulations showed that high winds, blowing over a hangar, caused a dynamic load on the parked aircraft and damaged an elevator actuator which caused the right elevator to remain jammed in a nose down position.
The write up, pictures, CVR transcript, and the NTSB praise of the flight crew's professionalism is a really interesting read. Those two pilots likely saved the lives of the University of Michigan men's basketball team.
https://www.ntsb.gov/news/press-releases/Pages/NR20190307.aspx
Here's the full report:
https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR1901.pdf
"Undetectable damage" to the aircraft prevented it from being able to fly. The Captain didn't realize it until he tried to rotate, then shut her down. His checkpilot scolded him for aborting above V1, but didn't try to override. They went off the end of the rwy.
Later inspections and wind tunnel simulations showed that high winds, blowing over a hangar, caused a dynamic load on the parked aircraft and damaged an elevator actuator which caused the right elevator to remain jammed in a nose down position.
The write up, pictures, CVR transcript, and the NTSB praise of the flight crew's professionalism is a really interesting read. Those two pilots likely saved the lives of the University of Michigan men's basketball team.
https://www.ntsb.gov/news/press-releases/Pages/NR20190307.aspx
Here's the full report:
https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR1901.pdf