inflightfailure
Filing Flight Plan
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- Aug 6, 2021
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inflightfailure
Hello everyone. I'm knew here. I'm trying to fact check a story going back to the late 70's. I'm hoping some of you pilots here can help me determine if this story in question lines up. Here are the details.
Man (not a pilot) claims to be on a short commuter flight in a small twin engine plane in which one of the engines had "exploded" and caught on fire. He describes a steep spiral decent which extinguished the flames. The plane then made a safe emergency landing.
Digging into this, there is no NTSB report on this incident. However, I did come across a snippet from a "Civil Aeronautics Boards Report". The date in question from the report lines up with the story, so I believe that this report is describing the incident in question.
"Incident occurred Nov. 11, 1976 involving Piper PA 31 N74985. Pilot experienced rough engine on scheduled flight fight between Salt Lake City and St. George. 3 Passengers on board. Engine was feathered and precautionary landing made at Delta Utah, per instructions in company manual. Investigation revealed cylinder base studs sheared. As result of occurrence Sky west changed maintenance procedures by checking torque studs at each 100 hour inspection. No damage to aircraft. No injuries to crew or passengers."
So, here are my questions.
1) Does the "story" seam to match the report?
2) What would happen if the cylinder base studs sheared? Would this just cause a loss of power? Rough engine? Oil leak? Could this potentially cause a fire?
3) Is the man telling the story exaggerating some of the details here (i.e. fire/steep spiral dive)
Thank you in advance for your comments and responses.
Man (not a pilot) claims to be on a short commuter flight in a small twin engine plane in which one of the engines had "exploded" and caught on fire. He describes a steep spiral decent which extinguished the flames. The plane then made a safe emergency landing.
Digging into this, there is no NTSB report on this incident. However, I did come across a snippet from a "Civil Aeronautics Boards Report". The date in question from the report lines up with the story, so I believe that this report is describing the incident in question.
"Incident occurred Nov. 11, 1976 involving Piper PA 31 N74985. Pilot experienced rough engine on scheduled flight fight between Salt Lake City and St. George. 3 Passengers on board. Engine was feathered and precautionary landing made at Delta Utah, per instructions in company manual. Investigation revealed cylinder base studs sheared. As result of occurrence Sky west changed maintenance procedures by checking torque studs at each 100 hour inspection. No damage to aircraft. No injuries to crew or passengers."
So, here are my questions.
1) Does the "story" seam to match the report?
2) What would happen if the cylinder base studs sheared? Would this just cause a loss of power? Rough engine? Oil leak? Could this potentially cause a fire?
3) Is the man telling the story exaggerating some of the details here (i.e. fire/steep spiral dive)
Thank you in advance for your comments and responses.