bigred177
Cleared for Takeoff
So over a year ago or so my mom's Navigator started throwing a P0308 misfire code. I pulled the coil and boot out and the boot was wet. After some research I found out is was a somewhat common issue, but that if you just kept blowing it out, it would be fine until it filled up again. So that's what I've been doing on a periodic basis.
Since I'm fixing to leave for training and won't be available I decided to go ahead and fix the issue. I thought the problem was that the lower intake manifold gasket was leaking coolant into the dwell. After tearing into it a little I just can't see how this is happening, and I can't justify tearing deeper into the engine until I can reconcile that in my head. I posted this on Ford Truck Enthusiasts but they have been slow to answer, the car is half apart, and she needs it. Everyone here has always been the most helpful even in things unrelated to aviation so I want to post the posts and pictures here and see if anyone has dealt with this or a similar problem.
Since I'm fixing to leave for training and won't be available I decided to go ahead and fix the issue. I thought the problem was that the lower intake manifold gasket was leaking coolant into the dwell. After tearing into it a little I just can't see how this is happening, and I can't justify tearing deeper into the engine until I can reconcile that in my head. I posted this on Ford Truck Enthusiasts but they have been slow to answer, the car is half apart, and she needs it. Everyone here has always been the most helpful even in things unrelated to aviation so I want to post the posts and pictures here and see if anyone has dealt with this or a similar problem.