Ghery
Touchdown! Greaser!
- Joined
- Feb 25, 2005
- Messages
- 10,944
- Location
- Olympia, Washington
- Display Name
Display name:
Ghery Pettit
My son and I went to the airport after work to grab the Arrow and fly up to PWT for dinner. Preflight went fine and the engine fired right up. Got cleared to rwy 26 and taxied down to the run-up spot. All was going great until I checked the mags. R - OK, L - 200 to 300 rpm drop and rough (max is 175 rpm and both should be within 50 rpm of each other). Tried leaning the mixture to burn out whatever might have been fouling a plug with no success. Each time I went to L and back to Both there was a pretty good bang. Rats. Called the tower with a change of plans and went back to the hangar and put it away. Called the maintenance officer to report the problem, wrote it up in the log and went home.
Nice clear day (too hot, actually). Would have been a lovely flight to chase some of the best fish and chips in the state. However, when the run up is so bad that one's non-pilot son notices the problem, there really isn't a doubt about what to do, now is there.
Oh well, gave me time to fix a software problem on my computer and a more leisurley packing for a trip to Chicago tomorrow.
Nice clear day (too hot, actually). Would have been a lovely flight to chase some of the best fish and chips in the state. However, when the run up is so bad that one's non-pilot son notices the problem, there really isn't a doubt about what to do, now is there.
Oh well, gave me time to fix a software problem on my computer and a more leisurley packing for a trip to Chicago tomorrow.