Richard Fry
Filing Flight Plan
- Joined
- Dec 23, 2016
- Messages
- 4
- Display Name
Display name:
RFRY1
The mix control cable on my 182 was stuck so I removed it and cleaned it. after reinstalling it to carb. the exh. temp rose to the top of 6probe egt.and stayed there throughout a 2000' climb out.
Returned to airport and checked the mix connection on carb. looked worked great on ground.
Departed again and same problem...
about a week prior to this I had a problem with starting after shut down. flew to lunch, after 1hr. went to leave and the engine would not start. ( 5000'alt. and about 50 dg). pulled mix out and it fired, enriched mix and ran great. after landing tried to start it again and same problem..
An a-p suggested replacing the needle seat float valve..
Not sure what the cause is but sure could use some ideas..
Returned to airport and checked the mix connection on carb. looked worked great on ground.
Departed again and same problem...
about a week prior to this I had a problem with starting after shut down. flew to lunch, after 1hr. went to leave and the engine would not start. ( 5000'alt. and about 50 dg). pulled mix out and it fired, enriched mix and ran great. after landing tried to start it again and same problem..
An a-p suggested replacing the needle seat float valve..
Not sure what the cause is but sure could use some ideas..