MauleSkinner
Touchdown! Greaser!
Also the rubber gasket on the right wing fuel cap was not installed.
According to company and airport employees at Chester County G. O. Carlson Airport (MQS),
the pilot arrived around 1230 and made it clear that he was “in a hurry,” as he had a return
flight from Knoxville, Tennessee, booked for 1800 that evening. He called the fuel truck
multiple times and indicated to the linesmen that he was in a hurry and was not pleased with
their delayed response to his fuel request. The airplane’s 116-gallon fuel system was serviced
with 80 gallons of fuel, which reached “to the tabs” in each fuel tank.
According to witnesses and surveillance video the pilot did not obtain fuel samples from the
airplane’s fuel tanks prior to takeoff.
Yep....no new ways to kill ourselves.The right engine carburetor was disassembled and revealed an intact float. The mixture arm,
mixture cable, and throttle arm were all secured to the carburetor. Fuel drained from the bowl
was blue in color and contained visible water and debris. The fuel was tested with waterdetecting paste, which detected water.
Both the left and right-side fuel boost pumps, one in the root of each wing, were energized with
a battery, and both pumped fuel from their respective sump tanks immediately adjacent. Both
fuel samples contained water and debris.
Samples taken from the sump tank, engine-driven fuel pump, and the carburetor bowl on the
airplane’s right side all contained water and debris.
The rubber gasket on the right-wing fuel cap was not installed.
But he had qualified for BasicMed last year."His most recent Federal Aviation Administration (FAA) third-class medical certificate was issued on November 1, 2007."
ah. so there's nothing on your record about basicmed? I guess not.....But he had qualified for BasicMed last year.
It was noted in the report.ah. so there's nothing on your record about basicmed? I guess not.....
if basic med is documented in a similar manner as class I/II/III, why would the report even need to mention his last class III ? seems odd. why not just say he was current with basic med?It was noted in the report.
Why say there was no water in the left engine carburetor?if basic med is documented in a similar manner as class I/II/III, why would the report even need to mention his last class III ? seems odd. why not just say he was current with basic med?
because it's relevantWhy say there was no water in the left engine carburetor?
I guess relevance depends on perspective. Apparently the NTSB thinks the background qualifying him for BasicMed is relevant.because it's relevant
Based on findings discussed on page 3, looks like another ~20 sec and the left carb would have filled up with debris and water and failed that engine as well.Why say there was no water in the left engine carburetor?
The statements about pilot medical qualifications are also facts.The whole point of the prelim is to state the facts. Left carb did not have water. The right did. The right tank didn't have a gasket.
I’m with option one of those are the only choices.So was our influencer friend, presumably watching this go down, thinking "oh no I may have killed someone" or "oh man this is gonna get so many views"
The work included, but was not limited to, propeller governor rigging (both sides), the left side fuel quantity indicating system, alternator, alternator switch, and the left magneto on the right engine. The work was completed on the day of the accident.
I know someone who did do that and lucky for them the engine died just as they turn into the active.I've been told O-320s in Cherokees will make it pretty far into the takeoff process with the fuel valve set to OFF.
For a plane that sat for a couple years, it's mind-blowing that they didn't give the fuel system a good look. I wonder if it was sheer luck that they didn't have a fuel-related failure on the way from Michigan, or if the water/debris was was introduced during/post maintenance in PA.I had actually wondered when I watched these episodes if they ever went thru the fuel system from tanks to carb. There was nothing in the videos that suggest they did.
Based on the water and "detritus" in the fuel system I doubt they did. Water could have been picked up by the recent refuel, but detritus not likely.
It’s almost as if they followed the model of barn-find cars you see these days-fresh gas, new plugs/wires/cap/rotor, new battery, new oil/filter, and let ‘er rip.For a plane that sat for a couple years, it's mind-blowing that they didn't give the fuel system a good look. I wonder if it was sheer luck that they didn't have a fuel-related failure on the way from Michigan, or if the water/debris was was introduced during/post maintenance in PA.
Based on what they found in the fuel system so far, I think the balance shifts more towards the "they didn't do it" end.One thing to remember is youtube videos are edited for effect and not always for full context of the project and could be missing the some of the items mentioned above. Regardless, this same type scenario plays out in the real world more often than some people realize, and on occasion ends in the same manner. No youtube channel needed.
I'm pretty sure his first thought was "I'm done, they'll sue me out of existence". I don't see a way that he can recover from this.So was our influencer friend, presumably watching this go down, thinking "oh no I may have killed someone" or "oh man this is gonna get so many views"
Maybe. Wouldn't be the first time an aircraft that sat unused for extended periods had old, solidified deposits in the fuel system loosen up once it was serviced with fresh fuel. Sometimes even after several flights. I've also seen a shop towel eventually end up in an oil filter 120 hours after overhaul and 3 separate oil changes. Will be interesting what the factual and docket have to say.Based on what they found in the fuel system so far, I think the balance shifts more towards the "they didn't do it" end.
I'm pretty sure his first thought was "I'm done, they'll sue me out of existence". I don't see a way that he can recover from this.
I don’t see any reason to speculate on what anyone’s first thoughts were, let alone to impugn a man like that.
Being in a hurry has everything to do with YouTube... in this case, it would appear, as well as trying to hard to do something on a budget.I don't think this accident has anything to do with YouTube. The report indicates that repairs were made the day of the flight:
The work included, but was not limited to, propeller governor rigging (both sides), the left side fuel quantity indicating system, alternator, alternator switch, and the left magneto on the right engine. The work was completed on the day of the accident.
After such maintenance, it would be prudent to do an extended run-up, fuel sample, etc. Seems like that was not done. Again, nothing to do with anything except the PIC making some bad decisions, which started with not checking for water in the fuel and being in a hurry, ultimately leading to the tragic result.
In our amazingly litigious environment, it's one of the first thoughts people have when involved in serious mishaps. People have been sued for a lot less, and had to work hard to defend themselves. I think it was someone on this forum that had to put up with some guy renting (or stealing) a plane he was leasing back to a flight school, crashing it (on purpose?) and killing himself and his child. Took years to clear his name, and he was the textbook definition of being innocent. This is our wonderful (< - sarcasm) legal system, where such drivel can be brought in court and you have to spend your own money to defend yourself.I don’t see any reason to speculate on what anyone’s first thoughts were, let alone to impugn a man like that.
It has a lot to do with the youtube reality tv model. I bought "the cheapest plane on ebay". Can I "flip it for a profit"? Shoestring budgets and corner cuts don't do well in aviation. Especially when paired with lack of experience.I don't think this accident has anything to do with YouTube.
That's pretty wild speculation, especially since witnesses quoted the pilot as saying he was in a hurry because he had a return flight.Being in a hurry has everything to do with YouTube... in this case.
And why would the return flight matter if they didn't "need" to fly it that day? Why did they "need" to fly it if not for the cameras, and keeping interest on their project?That's pretty wild speculation, especially since witnesses quoted the pilot as saying he was in a hurry because he had a return flight.
"According to company and airport employees at Chester County G. O. Carlson Airport (MQS), the pilot arrived around 1230 and made it clear that he was “in a hurry,” as he had a return flight from Knoxville, Tennessee, booked for 1800 that evening. He called the fuel truck multiple times and indicated to the linesmen that he was in a hurry and was not pleased with their delayed response to his fuel request."
I suppose it doesn't matter why, though. As PIC, he bore all the responsibility for ensuring the plane was airworthy, and on that, he failed.
You're right - the PIC didn't NEED to fly it that day. Likely felt some pressure, though:And why would the return flight matter if they didn't "need" to fly it that day? Why did they "need" to fly it if not for the cameras, and keeping interest on their project?
I've done "test" flights before - on new engines for break-in, after heavy maintenance, and once on a "new" used engine installation on an RV-6 before a ferry flight. I've never ONCE been in a "hurry" to fly an airplane that I think has a higher probability of killing me.
As opposed to the narcissism involved in attacking strangers on an anonymous internet forum?